Investigation of double effect evaporation model to energy consuming reduction in NaCl production process: industrial case

سال انتشار: 1402
نوع سند: مقاله کنفرانسی
زبان: انگلیسی
مشاهده: 84

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شناسه ملی سند علمی:

ICIRES16_017

تاریخ نمایه سازی: 25 دی 1402

چکیده مقاله:

The experimental data of an industrial unit producing sodium chloride salt by recrystallization method with evaporative crystallization equipped with a thermo-compressor (TC) were investigated. The feasibility of replacing the proposed double effect evaporation (DEE) model instead of the current plan was modeled. The findings indicate that maintaining an equal amount of motive steam in both modes results in a ۴۴% increase in production within the DEE model. Furthermore, concurrent with the production increase, there will be a reduction of ۶۰ units in the specific consumption of natural gas fuel per ton of product produced. In the existing unit, due to the presence of a TC in the path of steam entering the heat exchanger, high pressure steam is needed, which in the studied industrial unit is ۱۰ bar; in contrast, within the proposed DEE model, the motive steam pressure is ۲ bar, as a result, approximately ۱.۸% less fuel will be required in the boiler to generate every ton of steam. These results demonstrate the potential for significant efficiency gains and reduced resource utilization by implementing the DEE plan within the sodium chloride salt production process

نویسندگان

Manouchehr Manouchehrianfard

Utility supervisor of ISM Company, Iran Salts Mining Company, Garmsar, Iran,

Farhad Mahmoudiyekta

Manager of ISM Company, Iran Salts Mining Company, Garmsar, Iran,

Ali Aghamohsenifashmi

Planning Manager of ISM Company, Iran Salts Mining Company, Garmsar, Iran

Bita Soleimani

Faculty of Chemical, Petroleum and Gas Engineering, Semnan University, Semnan, Iran